Need help with figuring out why the servos are going nuts with the new Tx and rx on the King 4. Bind went fine and all servos hooked into their proper channels, as soon as battery is hooked into the esc all four servos jitter and go to one side. Is there something I missed in the transmitter setup? Should I adjust the end points? I bought an rtf bird and this is my first run at a computerized controller. Any advice is greatly appreciated. Oops never mind should have been in ppm not pcm. Thanks anyway.